Coca Cola CHP installation
Coca Cola CHP installation
SCOPE
The scope of work included the installation of a 800Kw CHP system and 2 new 500bhp boilers at the Coca Cola bottling facility at 24 Fenmar Drive, North York.
ISSUE
Coca Cola was experiencing high electricity costs at their plant as well as a need for system steam within the existing facility.
ASSOCIATED OPPORTUNITY
- The combined heat and power unit will provide system steam and heat generating capabilities to the existing infrastructure. The new 500bhp boilers replaced 4 existing boilers to provide high pressure steam to the existing facility
- The new 500bhp boilers also provide high pressure steam for a new pasteurizing system implemented in the facility
- Improve efficiency of system boilers to support facility expansion requirements
- Reduce the electrical requirements for the facility on the local power distribution grid thereby reducing
electricity costs
KEY PROJECT COMPONENTS
- Turn key EPC project in collaboration with CEM Engineering
- Construction project management and managing site safety protocols, including site specific COVID 19 requirements
- Demolition work of 4 existing boilers and associated electrical/mechanical/piping
- Civil construction which included helical piers for the main engine compartment as well as the auxiliary
equipment compartment - Installation of temporary boiler and associated piping and electrical to support facility operation during
construction phase - Installation of 2 new 500bhp boilers along with associated electrical/mechanical/piping systems
- Installation of new Heat Recovery Steam Generator (HRSG), accumulator tank, condensate tank, hot water loop piping
and high-pressure steam header and piping to new pasteurizer system - Installation of natural gas line to CHP unit and new boilers
- Installation of 1600A bus extension from existing switchgear to new 600V 1200A generator breaker section
- Installation of associated cabling between new 600V 1200A generator breaker and CHP unit